I checked the taken images and confirmed that we don't need to update the reference positions.
I checked the taken images and confirmed that we don't need to update the reference positions.
ETMX is cooled rapidly (51K: 8K reduction from 59K last morning). So it is better to turn on the heater.
The increase rate of the EX BRT Head temp became so slow. The vacuum level at EXT is also very gradually increasing.
Just a report
I found that ETMX_TM_WIT_P suddenly oscilated when only X-arm locked. Judging from the timeseries of WIT_P_DQ, the oscillation frequency seems to be 7.44 Hz. It is Pit resonance. Today, since there is OMC REFL work, X-arm has locked and ETMX has been LOCK_ACQUISIION from morning, Fig. 2 shows the 11 hours trend. ETMX_TM_WIT_P seems to raise up occasionally.
Michimura, Tanaka
## Abstract
We completed the alignment of the OMC REFL path and their characterization (TFs and phasing). Also, we installed the BS (R:T=90:10, Thorabs BSX11) for the QPD protection from 10W lockloss.
## What we did
At 20:23:32 JST, ETMY was tripped suddenly and went to PAY_TRIPPED. At this moment, H3_RMS value seems to jump third time (fig.1), and surpassed the thereshold of WD at last (fig.2). After that, the H3 signal in view of K1:VIS-ETMY_IM_OSEMINF_H3_OUT16 seems to be strange compared with other sensors' outputs (fig.3). Fig.4 is the same signals 17 days before in PAY_FLOAT. Current, H3 seems not to observe ETMY motion for some reason.
I'm not sure how to deal with it, so I leave it tonight.
I started the lockloss investigation on 2025/03/05 8:58 UTC ~ 20:45 UTC. Previous lockloss investigation was posted in klog32803.
During this period, there were 18 lockloss. The plots are summarized in wiki.
Just before the lockloss, we observed the saturation of both OMC PD. In the previous investigation, we saw similar saturation with reducing the AS 17 (which indicates the reducing of the optical gain). But, this time, we did't see such reduction. The AS17 signal looks healthy.
Although the OMC PD signal was oscillated with 20 Hz in most lockloss, the amplitude was not increased. As I heard from Ushiba-san, this frequency came from the suspension and is not related to the lockloss. Figure 1 and 2 show the example.
For futher investigation, I checked channels related to OMC LSC control (Figure 6). One finding is that the typical value of K1:OMC-TRANS_DC_DIFF_OUTPUT is -0.45, which is different from the previous typical value. For example, the value of 12/17 is -0.26.
After reparing the OMC PD B, we did't perform the dark noise subtraction. We need to do it in future. But, as chated with Ushiba-san, this will be not the cause of the lockloss.
Although I checked the channels to monitor the mirror motion, I didn't find the strange motion. I plan to compare the spectrum of OMC PD B is same as previous.
Probably this is not the cause of the lockloss. But, I found the sudden drop of ISS feedback signal (K1:PSL-ISS_FIRST_SERVO_AOM_MON_OUT_DQ) and K1:LAS-POW_PMC_OUT_DQ, even though the error signal of ISS was not changed.
Figure 3 and 4 show the examples.
One lockloss was caused by the 1 Hz seismic motion. That makes the 4 Hz oscillation of the feedback signal of IMC length and IMC lockloss, as shown in Figure 5.
## Abstract
I completed the replacement itself of OMC REFL QPDs but the alignment of OMC REFL path is on going because I found that the beam position on the upper mirror of the periscope is shifted. Also, the characterization of replaced OMC REFL QPDs is necessary.
## What I did
## Next
With YamaT-san, Oshino-san, and Marco-san
We are maintaining the existing network configuration of cal-gst0 and cal-gst1 while enabling the test server, cal-gst0, to run the cal pipeline for testing Kafka and other components. Today, as part of the preparation, we copied the missing data from gst1 to gst0.
For the time being, we will maintain the current network configuration and proceed with development and testing of Kafka on gst0. The current network configuration allows gst0 and gst1 to have different IP addresses on the DGS network, enabling access to GitHub and other necessary resources.
Our goal for this week's work is to run the calibration pipeline on gst0. To achieve this:
We confirmed that data1 on gst1 is used in the pipeline.
Currently, data1 on gst0 was initially empty.
We copied data1 from gst1 to gst0, and this task has been completed.
Now that the data copying is complete, we have started testing the pipeline on gst0. The next step is to verify that the pipeline runs successfully and to troubleshoot any issues that arise during execution.
Memo:
cal-gst1 = Production server
cal-gst0 = Test server
I checked current OMC ASC performance and found that the performance is not good due to two reasons: CARM offset value and ISS.
So, I modified INITIAL_ALIGNMENT guardian and CARM offset,
It improved the SNR of dither lines by a factor of 10, so it would improve the alignment to OMC.
Recently, even performing initial alignment to OMC, alignment to OMC with PRFPMI seems not good, whcih prevented the stable lock.
So, I investigated the reason why the initial alignment doesn't have good performance.
Figure 1 shows the OMC trans PD spectrum when INITIAL_ALIGNMENT guardian was at ALIGNING_TO_OMC.
Blue lines show the spectrum of OMC trans PD signals with the current nominal condition for initial alignment.
Green lines show the spectrum with ISS, which improved the noise floor by a factor of 2 aaround dither frequencies (13-17Hz).
Brown lines show the spectrum with ISS + manual tuning of CARM offset, which improved the noise floor by a factor of 5 around 10Hz.
So, I changed the CARM offset value from -0.8 to 6.7initial alignment.
I also modified the INITIAL_ALIGNMENT guardian to turn on ISS for OMC alignment.
I haven't checked it improves the alignment to OMC, so it should be checked with IFO.
I also modified the OMMT2T trans QPD loops to reduce the jitter noise during initial alignment, which might be contaminated the OMC trans PD spectrum according from the OMC commissioning in 2024 (klog30453).
Figure 2 and 3 show the OLTF of pitch and yaw loops, respectively.
Though they are not drastically changed, gain peaking around UGF becomes small while keeping the larger DC gain, which would reduce the rsidual motion of beam spot on OMMT2.
[Ushiba, Kenta, Yuzu]
This is a report of last Friday.
During the lockloss investigation (klog32803), we found the strange causality about the IMC and LSC_LOCK guardian and K1:IMC-CAV_IS_RESONATING channel. I guess this strange causality is not related to the lockloss. For the future works, I put the memo about this phenomena. Although we checked the data, we are not sure the cause.
Yesterday I replaced the connectors from the AI chassis (D-sub 9) to the PEM injection amplifiers to the pannel type ones.
I prepared a new model library of the common mode servo on which the latch system was applied to all IN1, IN2, and FAST gains (see also Fig.1).
The latch system was already applied only to IN1 for IMC and CARM servo as shown in Fig.2 and it works fine. So this new model should help to mitigate a loud glitches coming from a timing gap between turning on and turning off of BIO and probably allow to change a gain also for IN2 and FAST as 16dB <-> 15dB and 7dB <-> 8dB with keeping IR lock.
For applying this new model to CARM servo (= k1alspll), we need to take care about Dolphin issue. So I haven't installed the new model yet. It can be applied on next maintenance day.
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An amount of the timing gap is slightly different in each BIO card. So a waiting time on the latch system was implemented as a variable named as K1:***-SERVO_BO_DELAY_N in the past work. Though I had considered to prepare independent 3 variables for IN1, IN2, and FAST gains, one variable should be enough because one common mode servo is driven by using one BIO card. So in this update, an amount of the waiting time is a common variable for IN1, IN2, and FAST gain.